As I was leaving the safety seminar a couple of weeks ago, Dave Jones stopped me and asked about the knocking noises coming from my engine. I didn't have much to say other than the engine was very tired and would need a rebuild soon. But I did notice that as I drove away, Dennis Rinaldi had a very concerned look on his face. The next day Dennis called and strongly suggested I not drive the car again until we had a chance to take a closer look at the engine because it sounded like I had a connecting rod problem. And so began my connecting rod adventure.

I dropped the oil pan to see if there were any bits and pieces of babbit from the rods or main bearings in the pan, luckily there wasn't anything obvious. There is some braising in the dip pans where there may have been rust spots or holes previously drilled in the pan, but that's it.
The oil pump stayed up in the block, so I left it there for Dennis to see. When he came over a few days later, the first thing we did was to remove the pump. Well, we both looked at it and we noticed it didn't look right and sure enough, the top 1 inch of the pump stayed up in the block. Luckily because it was only the top part of the pump and

the spring was holding it in place, oil was still getting into the engine just fine. My dad gave me a bunch of extra engine parts when he gave me the car, and among them was an oil pump with the screen cover missing. Ted Kafer was kind enough to donate a cover for me so I now have a complete replacement pump.
It's a little scary seeing my engine with it's bottom exposed, wondering if I'll ever get it back together again. The engine was nice and clean inside. My dad had dropped the pan when he rebuilt the car and cleaned it out really well.
We worked our way through the connecting rods for pistons 1, 2, and 3. Taking them loose, inspecting them for cracks or missing bits of babbit. Each had a single shim which needed to be removed. On a couple of the caps, we had to file them down to get the proper clearance on the crankshaft when we torqued them back on. I now know how to use plastigauge, I'd heard about it, but never used it. One of the many things Dennis has shown me.
For all the pistons, we did notice a bit of slop in the wrist pin bushings. This could very well be the source of some of the engine noise I'm experiencing. Well, since we were on a roll, we continued onto cylinder #4. As soon as we removed the connecting rod cap, Dennis noticed a large chunk of babbit stayed behind on th

e crank shaft from the connecting rod side. That pretty much put a stop to any more work that night, and we were making such good progress too. We decided the next step would be to remove the rear main bearing cap, if that was busted up, then it would be time to rebuild the engine, if not, then we would proceed with replacing the connecting rod from below, at least that would be our goal.
Fast forward a few days and Dennis came back to help check out the rear main bearing. He brought along an original Ford wrench designed for just that purpose since it's a very tight fight for modern torque wrenches. We took off the cover plate, then removed the nuts for the rear main - the decisive moment where I either rebuild the engine, or eek a few more miles out it was at hand.

We pull off the bearing cap and.... it's fine and in good shape. No cracks, chips or missing pieces. Whew! No shims though, so it's nearing the end of it's life.
Now to tackle that pesky #4 connecting rod. It's a tad bit easier with the rear main removed, we don't have to worry about breaking off the oil tube.
Dennis kept reassuring me that it's possible to drop the piston low enough, without exposing the rings, to remove the keeper snap rings for the wrist pin, then slide out the wrist pin, and remove the connecting rod. Sounds doable, but would my car cooperate?

We turn the crank into just the right position to gain maximum access to the wrist pin. Pull out the keeper rings and start working on the wrist pin. Over time, a shellac builds up on the wrist pin in the exposed areas which makes removing the pin difficult. After much coaxing, stuck fingers and no so gentle persuasion, we managed to get the wrist pin out. Success!

Look at that, no wrist pin or connecting rod in the piston!
A side note: While we were busy getting the wrist pin out, every once in a while, a drop of water would hit the floor. We finally tracked it down to a potential small leak in the head gasket at cylinder 3. There's no water in the oil, so I'm confident I don't have a cracked block. A bit of radiator stop leak will hopefully fix that.
As I mentioned earlier, my father sent along a bunch of extra engine parts, included in that list are two crank shafts, 4 pistons, and 8 connecting rods. We mic'd out the crankshaft from my engine, then measured the other two other crank shafts. Well it turns out that one crank is almost an exact match and it had 3 connecting rods still attached. We removed the rods and after inspecting each one, found one that looked pretty good. It measured out to be within 1 -2 thousandths of the original. Talk about lucky.
Because of the slop in the wrist pins, Dennis suggested we remove one from an extra piston and see if it was any tighter fit. We took one out and yes, it was a better fit in the connecting rod, but when we attempted to push it back into the piston in the engine, it was just a bit too tight, so we went back to the original wrist pin. The new connecting rod did fit a bit tighter on the original wrist pin anyway. The keeper rings for the wrist pins were a bit of a challenge to get back in, but perseverance paid off.

We torqued up the connecting rod and it was a perfect fit with no shims, just like the rest of the rods. I now have a 4 piston engine again.
When I dropped the oil pan, most of the gasket stayed up on the block. So the day after we got the rod back in, I spent a couple of hours under the car cleaning the old pan gasket off and scrubbing the gasket surface clean in preparation for putting the oil pan back on.
Today (20th), I decided to plastigauge out the rear main, Dennis is busy, so I'm on my own. The problem is that I don't have the special ford wrench and it's a tight fit for modern wrenches, but here again I lucked out. The rear main cap for my engine is one of the 'thin' boss type, which makes it easier to fit wrenches in. My 1/2" torque wrench with a standard 3/4" socket JUST fits inside the opening. I torqued it all up to 75 lbs, took it off and it measured out to 1.5 thousandths. Almost perfect. I shined up the surface of the cap, oiled the bearing and torqued the cap back on. The castle nuts even lined up with the hole in the bolt for the cotter pins. I'm almost there.
So what's left? I need to torque up the connecting rods, put in the cotter pins and make sure the engine still turns. Once that's done, then it's a matter of putting the oil pan back on, oh, and add some oil too. I'm definitely past the hard part. I should be back on the road soon!
Even with all this tightening up and the replaced connecting rod, I know I haven't eliminated the need for an engine rebuild, but I've hopefully delayed it for a few more miles.
I can't thank Dennis Rinaldi enough for his help, patience and support during this whole ordeal!